you see now i personally like the look of the square headlights.
anyway, we got a chance to work on it a bit the last couple of days. first I used three cans of degreaser and a lot of hot water to clean it up some. it could still use a trip to the car wash and a nice long washing with a pressure washer but it is a lot better.
then we put the fuel pressure regulator on and set it to 3 psi.
next we did a nutter bypass since the carb was already swapped to a weber.
then we removed the egr valve since it had already been disconnected and made a block off plate for it.
then we spent a lot of time trying to sort out what the heck had been done with the vacuum lines, and plugged all the spots that were not connected right. ran a new vacuum line to the distributor area.
swapped in a rebuilt distributor that had the vacuum advance. at this time we found out that the old distributors vacuum advance had just been broken off and the part inside the cap was just flopping around in there. no wonder it ran like crap. new cap and rotor,
then we tried to start it. here is what it sounded like on the first attempt.
set the timing to 8 degrees btdc, awesome. it now runs and idles pretty darned good. then we put a new set of plugs in and did some adjusting of the carb. and took it for the first test drive. drove all the way across town.
then we discovered several other things lol. first the front end needs some serious work. the steering box is really loose, we will try to tighten it but will most likely end up swapping it at some point.
second the water temp gauge doesn't work.
third the heater never did heat up, and the fan would not shut off.
when we got back to the shop we let it run for a while while we used an infrared thermometer to measure temps at the intake manifold and the hoses and found that the engine was not getting up to temp. we also at about the same time checked out under the dash to be sure there was not a vacuum activated water shut off. there wasn't.
so we figured the thermostat must be stuck open. drained all the nasty rusty disgusting water out and found that was not the case. there was no thermostat at all. so we went and got a new 190 degree thermostat and I cleaned up the thermostat housing. then My Dad wasn't feeling well so he went home. I then did some more work under the dash. I figured out that there was a spring that was dislodged in the switch assembly and it had gotten wedged in between the contacts that were supposed to shut off the fan. got that fixed. then I quit for the night also. I still need to figure out what is wrong with the temp sender. when dad comes back tomorrow we will ground out the sending unit wire and see if the gauge moves.
and put the new thermostat in and fill it back up. oh btw I also blew through the heater hose and water moved through it so I know it is not blocked. I should probably flush that with water tomorrow before I put it all back together.
anyway the thing is coming together pretty good so far.